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| Foundation
of pot furnace being laid at site |
Intervention
in pot furnace
There are nearly 80 pot furnace units operating in the cluster.
Taking up the challenge of fuel switch-over, the project developed
and demonstrated an energy efficient NG (natural
gas) fired pot furnace in a working unit at Firozabad. The
demonstration plant was commissioned in February 2000. It was an
instant success in terms of achieving significant reduction in energy
consumption. However, the furnace had to be fine-tuned and modifications
made in the various sub-systems to optimize its performance. The
demo system showed significant fuel savings (56% reduction in energy
consumption as compared to coal fired furnaces and around 30% as
compared to conventional NG fired pot furnaces). The special features
of the demonstration pot furnace are
use of waste heat
recovery system (a metallic recuperator with 5-pass, made of stainless
steel/mild steel) to trap heat in flue gases for preheating combustion
air,
proper fuel-air
mixing for optimal combustion conditions, and
prolonged life of
various furnace sub-systems.
Intervention in muffle furnaces (pakai
bhatti)
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| Demonstration
Gas Fired Muffle Furnace |
There are more than 700 pakai bhatties operating
at various locations in Firozabad. These bhatties are highly
polluting and a majority of them are located in congested residential
localities in the heart of the city. Pakai bhatties are
presently the largest consumers of coal—estimated to be around
100 000 tonnes per year—in Firozabad. These are very small
units and are not registered under the SSI (small scale industry),
hence, no clear database of this industry segment was available.
To get ideas on possible design options for energy
efficient muffle furnaces, the project initially conducted a design
competition by seeking concepts from various sources. Based upon
the responses received, three ideas were short listed and further
investigations undertaken to design optimized systems. Considering
the nature of the industry and the financial capacity of the owners,
it was decided that the new design should not be a major deviation
from the existing design—mainly in terms of the operating
practices. Hence, TERI worked closely with the muffle furnace operators/entrepreneurs
and developed a NG fired pakai bhatti, which was demonstrated
to the cluster in August 2001. The energy consumption was nearly
40 % less than the coal fired furnaces and there was a drastic reduction
in the local air pollution, mainly due to the use of the cleaner
fuel, viz., natural gas.
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